Tuesday through Thursday was light air with 10-14kts of breeze, occasionally dropping to 6-8 which forced us to motor for a few hours. We got pretty complacent with the light breezes, excited when it would surge to 16kts and we would have a little more speed.
Our 24 hrs begins on Thursday afternoon when we decided to take advantage of the benign conditions and try our spinnaker furler system. Some suggestions had been made in Antigua after our testing there and we wanted to try them out. It was our first "solo", just Fay and I raising the big sail. We made the changes we discussed earlier and soon had it flying. We immediately picked up 1.5-2kts of speed and the boat felt much more stable. But after about 20minutes we noticed a problem with the furler which we thought was from our inexperience. We furled the sail (the problems with spinnakers are usually getting them down), but noticed another problem. We sorted those out, unfurled again about half way and then realized that the changes we had agreed to in Antigua (adding a snap shackle to the tack of the furler) were the cause of our new problems. So we furled it back up, sorted it out, and put it away for another day.
We had a load of wash going so Fay pinned the laundry up on the lifelines and we coasted along with our 12-14kt breeze.
Late that afternoon the forecast was for the breeze to freshen to 16-20kts in the evening and through the next morning so we looked forward to a little more speed. Just before Fay went off watch at 7pm we reefed the main just to keep things nice and mellow. It stayed light and in my 8pm log entry I wrote that we were "underpowered". But the breeze built as expected and we were soon moving right along. Then the seas built rapidly and we were very uncomfortable with a big cross swell that rolled us pretty wildly every 5 minutes or so.
I was awakened at 1:30am during Fay's watch when it was really rocking. We had 25-28kts, big seas rolling us like crazy, a lightning storm overtaking us from windward, and a ship which would not respond to our radio calls, had the dimmest lights I'd ever seen on a big ship, and was calculated to cross us with just 500yds to spare, way too close. The direction and force of the wind was sort of locking us into a "close call" course so we rolled up the jib and double reefed the main, allowing us to alter course enough to clear the ship by 2 miles.
But the big seas continued to roll us wildly and we sailed for some time with the double reef and a little bit of jib to balance the boat. Fay got some sleep and I was on watch until she came back at 6am.
I slept about an hour, then was awakened about 7:30am when New Morning took a hard turn and luffed up into the wind. I stuck my head up in the companionway and Fay told me the autopilot had quit working! Deja vu, this is what happened during our passage from Bermuda to the BVI's in 2008! I was barely awake but put on my PFD/harness and tether and confirmed she was correct, no autopilot. Plus some strange clunking noises, but the steering seemed ok.
Unlike our Bermuda/BVI passage, the seas were too rough to do anything immediately. Even though we were both exhausted, the only real choice was to hand steer until things calmed down. I did a quick weather check and concluded that the breeze should lighten up by early afternoon, and would be even lighter if we turned towards the Columbian coast. Columbia was not our destination so we split the difference and headed towards the coast, but not quite directly. Over the next four hours we took turns steering for 30 minutes at a time. In the 30 minutes when we weren't steering, we took turns hauling things out of the aft cockpit locker, cleaning off the hydraulic fluid that was all over everything (one indication that something was very wrong), placing the stuff in plastic bags and stowing it in the forward cabin. Finally I was able to remove the panel in front of the steering.
I expected to see something bad, but I was really surprised to see a hydraulic ram, still attached to the quadrant, still mounted to a huge aluminum base, and dragging hydraulic hoses, swinging back and forth every time we turned the wheel. We don't know exactly what failed, but it looks like the port cylinder mount pulled out of the boat which is very strange. In due time I was able to remove the ram from the quadrant, and attach the spare ram which is mounted on the starboard side. All of this while we still had pretty good sized seas and 20-23kts of wind. This is kind of like bolting something to the steering wheel while you're friend is driving down a twisty mountain road with no brakes. My fingers were holding onto the cylinder fitting and trying to slide it onto the peg on the quadrant, while Fay was trying to coordinate her turns with me, but not lose control of the boat. Then once the fitting was on the peg, I had to slide on a large washer and a retaining clip. All of this at arms length, under the quadrant and in constant motion threatening to claim one of my fingers. But we got it done.
Then it took another hour to juggle the wiring to the autopilot (the switch installed earlier was not wired correctly), and then convince the autopilot to use the new ram without going through all of it's setup procedures. We skipped the "learning" procedure and went straight to "on the job training". By 1:30pm the autopilot was again steering and we were exhausted.
I made a couple of phone calls and sent some emails, then Fay let me go to sleep. When I woke up at 4:30, things were as mellow as could be. New Morning was cranking out 8-9kts in 18-20kts of breeze, sliding down much more friendly waves. The sky was blue and clear and the wind had shifted to allow us to steer directly for San Blas. And after all the light wind and too much wind and autopilot problems and course changes for ships, our ETA was Saturday morning, four days for 700 miles, a very reasonable 175m/day.
And we've received a response from the people who installed the autopilot and are working to coordinate logistics for the repair in Panama.
24 hours...